AppleTY
Donating Member
So I have bringing my Ty back from the dead slowly but surely.
Today I decided to check compression, change the plugs and check the timing. Compression was pretty good (148 - 132), but when I checked timing I found that it appeared to be about 16* advanced! (a good inch ahead of the indicator)
This was pretty surprising to me, but I thought it might explain why I wasn't really getting much boost (~10lbs) and the truck was feeling sluggish.
I undid the timing connection and dialed it back to 0*. The truck was barely able to idle! I reconnected the timing connector, cleared the DTC and took it out for a quick DM run.
It's like I have no power whatsoever. Strangely, DM shows it boosting all the way to 14psi, but it felt like the engine wasn't getting any of it! Any ideas on what could be wrong?
Here is what the DM run looks like at WOT now:
Here's what it looked like before:
Today I decided to check compression, change the plugs and check the timing. Compression was pretty good (148 - 132), but when I checked timing I found that it appeared to be about 16* advanced! (a good inch ahead of the indicator)
This was pretty surprising to me, but I thought it might explain why I wasn't really getting much boost (~10lbs) and the truck was feeling sluggish.
I undid the timing connection and dialed it back to 0*. The truck was barely able to idle! I reconnected the timing connector, cleared the DTC and took it out for a quick DM run.
It's like I have no power whatsoever. Strangely, DM shows it boosting all the way to 14psi, but it felt like the engine wasn't getting any of it! Any ideas on what could be wrong?
Here is what the DM run looks like at WOT now:
Here's what it looked like before: