NM_TY_Guy
Donating Member
On Sept 28 2015 I picked up 93 TY 0935 (Phoon as my black truck is already called Ty) in Abilene TX, at the time I was told the motor had been rebuilt and just needed finishing up the installation. Yeah so not the case also some cladding was damaged the drivers side rear to kick panels needless to say it needed some work and I figured it would make a good project.
Started off by tearing the "rebuilt" motor down and sent the block to the machine shop of course they measure it and recommended bore it .030 over decking the surface and line boring the the mains and turning the crank 10/10 plus forge pistons. This project got off track from the beginning I only wish I would've put eagle rods in to it at this point but at the time was tying to stick to something of a budget. I built the motor with probe forged pistons stock rods and crank 412 comp cam found some L35 heads with screw in rockers used comp cams self aligning roller tip rockers hardened push rods Alex's springs and retainers.
My goal was to keep it close to stock as I plan to drive it on weekends to shows and car runs and the such. I also added ARP head studs and misc Arp hardware fluidampr harmonic balancer powdercoating most parts ceramic coating the exhaust manifolds and crossover pipe. Rebuilt the whole front suspension upper and lower control arm bushings upper and lower ball joint new cv axels Eric Tinns posi front axel. might as well ad a 3k stall converter deeper trans pan and cooler while the motor is out right? Solid motor mounts Jeep steering shaft all the typical upgrades.
Cleaned and repainted the frame etc etc.... I've been slowly working on this thing for almost 2 years and am about to drop the motor in to place and reassemble the front end then change the fuel pump get everything wired/ hooked up order a turbo tweak chip and hopefully get it running by the end of summer if I dont take a 2nd part time job first LOL I will keep adding more pics and listing more parts I've used as I think of them.
Started off by tearing the "rebuilt" motor down and sent the block to the machine shop of course they measure it and recommended bore it .030 over decking the surface and line boring the the mains and turning the crank 10/10 plus forge pistons. This project got off track from the beginning I only wish I would've put eagle rods in to it at this point but at the time was tying to stick to something of a budget. I built the motor with probe forged pistons stock rods and crank 412 comp cam found some L35 heads with screw in rockers used comp cams self aligning roller tip rockers hardened push rods Alex's springs and retainers.
My goal was to keep it close to stock as I plan to drive it on weekends to shows and car runs and the such. I also added ARP head studs and misc Arp hardware fluidampr harmonic balancer powdercoating most parts ceramic coating the exhaust manifolds and crossover pipe. Rebuilt the whole front suspension upper and lower control arm bushings upper and lower ball joint new cv axels Eric Tinns posi front axel. might as well ad a 3k stall converter deeper trans pan and cooler while the motor is out right? Solid motor mounts Jeep steering shaft all the typical upgrades.
Cleaned and repainted the frame etc etc.... I've been slowly working on this thing for almost 2 years and am about to drop the motor in to place and reassemble the front end then change the fuel pump get everything wired/ hooked up order a turbo tweak chip and hopefully get it running by the end of summer if I dont take a 2nd part time job first LOL I will keep adding more pics and listing more parts I've used as I think of them.





