Re: Turbo 3800 blazer
there more people looking at this than I thought. that tractor has some torque lol.
So progress has slowed a bit over the last few weeks.
After dumping a gallon of water into the coolant through a maimed front cover gasket I noticed that the motor had became a bit noisier than before. Not running a pcv valve didn't seem to be helping..and the noise continued to get worse. Then I started throwing 20 psi at it and although it was making a ton of power, the noise started to get louder at a more rapid pace. Eventually that noise expressed itself as a bad rod bearing that let go during a highway run. Catastrophic failure would be a good way to describe it.
I wasnt all that sad about that motor. I had learned alot with it and in the process beat it to ****ing death. 90* advanced timing, -5 degrees timing, not having a working pcv system and cheaping out on a front cover seal had all lead to the death of that motor. With all of that in mind I have set out to not do that again.
fun listing of failures
cracked #5 piston (believe it happened after the -5* timing week, noted that it has gained some blow by, now I know why)
#4 rod broken in half
#4 exhaust valve bent
#4 pistion distorted from hitting head
#4 exhaust lifter destroyed
head gasket around #4 distorted from heat generated form spraying fuel into a dead cylinder
all exhuast valve seats melted (likely from the timing issues, 90* advanced and -5 *advanced makes bad things happen to exhuast seats)
camshaft taco'd (rod went through the block into the camshaft area and bent it)
camshaft keyway destroyed, leading to it loosing cam timing
all pistons had a cool notch in them from hitting the intake valves.
This motor did not seize, it was still running somehow. I had to shut it off.
I managed to get some pitty head work done on a new set for 100 bucks, I got a good deal on new cometic head gaskets for 75 bucks, and got a cam for 300. with these parts I was able to build up another motor that a friend gave me. Unfortunelty this motor was a gamble, as he had pulled it out of a gtp that was said to be good but not confirmed. we got the motor in and it had good oil pressure at cold start, but once it got hot it lost all but 20psi and we decided to junk it.
a week later RPM in flint had a L67 block sale and we picked up an 03 block out of a gtp that had caught on fire for $150 and we assembled that this last weekend. I started putting it in the truck and its almost ready to fire. With a couple of hours of work tonight I'll see what this motor looks like. If it doest work I'll be pretty let down, but we now have a few extras laying around so at least it won't be a hunt.
I made at least 550 whp on 20psi. I was limited to that pressure by my Lt1 stlye MAF only being able to barely understand that. Fromw hat I have seen these motors are capible of more, I just need to learn from the mistakes I made the first time.